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Align 700 gas conversion using the SPE-43cc gas engine from Cermark
 
 
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2-15-09 - The first start went well today. I removed the tail blades and the head completely. The first few starting attempts did not get the engine to start and I found a bad switch and replaced it. The engine is able to idle low, real low. I have not adjusted any needles yet, more testing with blades on soon. It seems to be running just a little rich, transition to mid throttle was smooth. There is more vibration during higher engine RPM. I can attribute some to carb settings and the fact that it is a new engine. I was taking the cylinder temperature on top of the head near the spark plug, I saw a maximum of 166 degrees. Again, this is a no load test so far. I am running 5:1 (90x18T) gearing with 1.25 module gears from SDP. This required a few hours of machining to adapt. The main was a couple of mm smaller and the pinion is a little larger than stock, so I had to slot the clutch holder bolts a few mm to compensate. The gears are 10mm thick at the face so I'm not expecting any issues there. I doubled the lower carbon brace to help cope with the extra vibration from a big gas engine. I had to notch the frames for the side mounted spark plug. The side frames have been reshaped also to make room for the larger fan and fan shroud. I had to make lots of trimming etc to handle the larger engine dimensions. For 3D, I would use the 28cc engine. This is a near future project that is almost a "drop in" conversion compared to the SPE-43 and the larger head. I am running a Century V4 muffler with the threaded insert removed to minimize exhaust restriction. The little can muffler that comes with the engine has an equal size outlet, the unknown is internal baffling.



2008 Mercedes C63 AMG -- A minor distraction
 
 


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6-2-08 - I was looking at them and getting ready to sell the Corvette to start the factory AMG ordering process when one became available after the person who ordered it walked away for funding reasons, (lucky me).

Sceadu EVO EX converted to a YS-61 with 7.25 gearing
 
 


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5-11-08 - I started the conversion after talking with a friend last weekend looking for more torque to use in some of the snake or other backwards maneuvers in a 50 size ship. I used a standard 90 mount and milled the lugs on the outside to match the width of the 50 size carbon frames. The motor sits low in the frames due to the overall length plus the bigger clutch. The slots were close but needed elongation to bolt the motor in place. I used a 90 size fan, hub, shroud with a 12T pinion for 7.25 gearing using 600mm blades. FAI style hovering at 1600 is smooth as silk and really locked in. Switching to idle up with the motor at a respectable RPM gives a head speed of 2310 and good torque. It tracks like a Pattern ship setup in low mobility in really fast forward flight.

The prototype eight blade head - version 2 coming
 
 


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6-7-08 - After some testing, I have decided to make a slight modification, full tests soon

5-24-08 - I had some time this weekend to finish up the head. The prototype is designed around the Align 600 upgrade blade grips to give the correct push rod clearances. I now have thoughts for a simpler easier to build design with more flexibility, planning to start work on it soon. In the mean time, I will test this unit for functionality, overall geometry and ruggedness. Making the adjustments to the swash plate for controling the head and the follower for phasing.

My e-Freya - 12S 4100 is giving 10 minutes of hover time.
 
 


4-27-08 - I needed a test unit for the 8 blade head under development and spent a couple nights installing a Neu motor in a Freya with some old parts I had laying around.

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On 12S using 12Tx95T, flat curves are at 50, 60 and 70 percent, head speed is 1700, 1800 and 1900. The main gear is still shedding under all this power leaving small white flecks everywhere. I will run 10S in the future.

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The funny thing is, it flies exceptionally well!



Avant with OS 1.60 glow motor
 
 
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4-19-08 - I managed a to get in a few tanks this weekend with a CY V3 Governor. The problem is keeping the muffler stabilized, the mounts are too susceptible to these vibration levels. I will either revise the mounts or weld the pipe to the custom manifold and eliminate the Viton o-ring system.

4-7-08 - On Saturday I had to take care of a loose fan - there is vibration. Sundays flights went well with some rolls, flips and FFF. It is almost impossible to set the throttle curves with this much power. I have a TJ Pro on the bench to setup on 15% Synthetic Morgan for the coming tests. Since it appears we have a predictable and strong motor candidate I have started to work on the 8 blade head. The drawings are completed and it's setup for 8 Align blade grips. The 3 inch cube of 6061 is on the mill, more chips this week.

3-30-08 - Sunday's flying was exceptional! This 1.60 is more like a tight .91 with the revised Dynatron. You must prime the 1.60 with a finger to the muffler for a few seconds to get it to start when cold. I went a screw driver blade richer on idle and it will sit there all day with big fin buzz at idle. Once in the air it seems to smooth out well enough, nothing has vibrated loose yet. The power is insane, although it isn't that much more than a well tuned 90. The torque factor is just unreal. The design of the 8 blade head is coming around to support a very large scale project in the future. The head temp after 6 minutes and 1/2 of the tank was only 160 degrees. I am getting 12 minute flights on the large EVO tank, but I don't remember how many CC's this is. I will go to lower nitro in testing over the next month while trying to find one of the CY governors.

3-29-08 - I was able to start the 1.60 today with the new revised starter and I was able to fly for some time before it went a little lean and I landed. All I can say at this point is WOW, the power and torque are off the scale!

3-16-08 - While waiting for parts, I moved on to the project that was next in line. The OS 1.60 glow motor is installed and running 5.9 to 1 gearing. The new motor mount blocks were milled from black delrin since this case is a little larger. The headspeed should end up around 1700 RPM running it just a little beyond the torque peak. Engine start today went well and with a geared starter, it didn't complain too much. It is running very rich at low throttle and blades off for this test. The engine temps at no load was around 110, most likely because it is cold and raining here this weekend. The first flight will have to be at the Las Vegas fun fly next weekend since I have to work next week.

Replaced the small starter with a Dynatron geared at 2:1
 
 
The little Century starter is impressive for it's size, but the 1.60 was to much for it and it went poof in Vegas. I had some SDP fairloc gears and was able to come up with a 2:1 gearing using 1 module gears. I milled the adapter plate and fitted the gears after drilling the centers of the gears to match the output shafts and milled the anti rotation pin slot.
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Avant with MVVS 26cc (1.6) gas engine - needs a new case
 
 
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3-9-08 I went back to the big muffler and transition was better without the tuned pipe effect of the muscle pipe. I had a problem with the muffler coming loose, seems the bolt head pulled through the mount perch??. The allen bolt snapped on removal (red loctite), so I drilled the head off and removed the muffler. Cut the remaining stud off and drilled for an easy out. No joy here as the case was damaged during extraction. Testing is on hold for the time being while I shop for a new case.

3-8-08 I was able to fly today, adjusting the low and high needles as I went along. There is a small transition problem with the muscle pipe and the engine temps are higher, I think the back pressure is too high. I got WAY to carried away and got the motor hot, although it was flying well up to that point. I will need to add the fan shroud base plate to see if this will improve the cooling.

3-2-08 Worked on the carburetor setup in conjunction with mounting the CY Muscle Pipe and had to move the choke to the right side for clearance. This gives a better fuel line routing, improved the pressure line setup from the crankcase nipple to the carb base and gets the choke lever on the cold side of the motor. Engine starts on Sunday afternoon 3-2-08 went well, requires a reset of the needles at the field next Saturday after chasing a gremlin.
MVVS gas engine -- 11 pounds ready to fly
 
 
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Testing is going well, 4 tanks burned during the middle of February. So far it is smoother than I would have expected considering it is still running a little rich. The temp gun shows 175 on the head and 135 on the case. I have switched over to a Century V3 muffler until I mill the adapter so I can run a Muscle pipe. This muffler is heavier than I would like, although it is very quiet. The power is good so far, hardly any change on a full pitch (12) climb out. No governor at this stage, still working on setting the needles.
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Electric Avant, 100cc Yak, Ducati and the Aprilia Dorsoduro
 
 
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Avant with a NeuMotor 2215/3Y and my Aeroworks 100cc Yak for IMAC
Avant with the OS 1.20 AX two stroke engine and 6:1 gearing - There is some vibration - adding a head gasket to reduce compression. The temperatures are normal with the engine in mid RPM and a 2000 headspeed.
 
 
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I have not been able to cure the primary balance problems by detuning the motor with lower compression. After nearly 2 gallons, this engine starts easily and will idle all day long. It is slow to transition into the mid range, but once there it is VERY much a torque motor. I still think there is potential because fuel consumption is better than a OS .91 SZ.
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Freya EX - revised with SSZ-3 head, extended boom and 810mm main blades.
 
 
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Running the softest damping and went to a 555 flybar up from a 490 and still have a little hula dance at low head speed.
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With these blades I can hit throttle hold land it and take off again, there is that much inertia in these 810 blades.
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Avant Zenoah G20 Gasser - February 2007
 
 
The Zenoah G20 is only about a 1/2 pound heavier than a OS .91. It is at least a half pound lighter than a standard Freya.
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These pictures show the left side carburetor setup, the servo is easy to setupwith a nearly straight connection.
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This is the earlier setup with the carburetor on the OEM side. I wanted to use the traditional throttle servo mount on the Avant and switched the cylinder to put the carburetor on the left side. This does require the piston be removed and rotated 180 degrees to keep the ring locater in the correct orientation.
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G20 Gasser 29Jan2007
 
 
The frames required a little modification here and there to give clearance for the larger fan and shroud to cope with the heat a gasser puts out in comparison to an alcohol setup. I moved the battery tray up to give better access to the spark plug. This mimics the method used on the Aurora by trimming the frames and drilling the cross block holes.
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Hirobo Sceadu 50 EX - This is the smoothest helicopter I have ever owned
 
 
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Other interests, Supermoto racing.
 
 
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Avant with the CarbonXtreme Programable Head.
 
 
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San Diego, California.
 
 
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...............................................................................................................................................................
Hirobo Freya Gasser Conversion
 
 
MVVS 1.6 26cc, reworked a 15T pinion and 91T main gear for a 6:1 gear ratio
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The mechanics are completed.
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Hirobo Freya WC skin for RealFlight G2 Foiler
 
 
Click the graphic for download:
Misc. Pictures
 
 
Going to a Fun Fly is fun!
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Pictures of my custom Sceadu with ECCPM
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I tested the SSR-V head on the Sceadu, awesome hover
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Here are a few pictures of my Hirobo Freya EX. There is a full gallery of pictures under the content banner.
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More R&D Projects
 
 
Here is the under slung version of the SSR-V head on the Freya EX.
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Other fun things from my past
 
 
Here is the VOR503 I raced during the 2000 season in Supermoto and the new 2006 Husky SMR510 I race now.
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